Home > Technical (L322) > 4.2 SC lean codes |
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Danwilderspin Member Since: 15 Jun 2016 Location: Cambridgeshire Posts: 2215 |
How are you getting on? Did you buy coils? I was thinking g if it were coils it would be running rich as there’s be excess unburnt fuel... Current stable:
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7th Jul 2020 9:14pm |
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mgrover Member Since: 03 May 2020 Location: Leeds Posts: 394 |
No real diff from changing the coils. On an unrelated note I installed new reducer, magic jet 3 power. That thing is good. So my lpg lean problems have gone away as well. I just need to install new injectors and get it calibrated.
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8th Jul 2020 7:05am |
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Danwilderspin Member Since: 15 Jun 2016 Location: Cambridgeshire Posts: 2215 |
Is it misfiring on both fuels? I can’t remember and through out the revs? I doubt it’s vsr in 3k miles especially if they used hardened seats there are people with 100k plus on here with hardened seats. Also you barely used lpg since it was done.
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8th Jul 2020 8:48am |
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mgrover Member Since: 03 May 2020 Location: Leeds Posts: 394 |
both fuels, but only at 2.5/3k rpm. doesnt occur at 2k rpm or 4k rpm. that graph above demonstrates it. i may do a compression check tbh, just to be sure. but if it was i assume itd be misfiring in all rev ranges. this feels like maybe the supercharger? since 3k might be when its spinning up the fastest or something like that? |
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8th Jul 2020 8:52am |
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Danwilderspin Member Since: 15 Jun 2016 Location: Cambridgeshire Posts: 2215 |
If you think that why don't you spill the belt off the charger and see if its still there? it won't be the super charger I doubt. Could be the elbow that dirty I'm not sure? I'm sure vsr is constant. maybe worth visiting a specialist if not? Current stable:
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8th Jul 2020 8:57am |
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mgrover Member Since: 03 May 2020 Location: Leeds Posts: 394 |
it might be worth going to someone tbh |
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8th Jul 2020 9:14am |
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mgrover Member Since: 03 May 2020 Location: Leeds Posts: 394 |
another update. so wanted to rule out the misfires, while at the lpg mechanic we did a compression test.
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17th Jul 2020 8:31pm |
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Danwilderspin Member Since: 15 Jun 2016 Location: Cambridgeshire Posts: 2215 |
Why can’t he wind the pressure down? Current stable:
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26th Jul 2020 10:44pm |
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mgrover Member Since: 03 May 2020 Location: Leeds Posts: 394 |
we limited the vacuum and that seems to of sorted the pressure issue. but we noticed bank 1 injectors had different timings to bank 2.
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27th Jul 2020 9:50am |
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Danwilderspin Member Since: 15 Jun 2016 Location: Cambridgeshire Posts: 2215 |
Cool did you clear the adaptations with the iid tool btw Current stable:
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28th Jul 2020 7:26pm |
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mgrover Member Since: 03 May 2020 Location: Leeds Posts: 394 |
yeahhh.
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28th Jul 2020 7:26pm |
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Danwilderspin Member Since: 15 Jun 2016 Location: Cambridgeshire Posts: 2215 |
Did you do what I said rag it about for about 20 minutes so the exhausts are pretty much glowing then crack them off? Mine wouldn’t do anything cold Current stable:
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28th Jul 2020 8:31pm |
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mgrover Member Since: 03 May 2020 Location: Leeds Posts: 394 |
its the precat ones i cant barely get my hand up there, let alone any leverage to crack em open Its actually a sport
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28th Jul 2020 8:32pm |
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mgrover Member Since: 03 May 2020 Location: Leeds Posts: 394 |
i smoke tested the brake booster, and mines leaking smoke i think thats why i have a lean code
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4th Aug 2020 4:45pm |
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