Home > Technical (L322) > 2004 V8 - Cut Out - Now Wont Start |
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dan_uk_1984 Member Since: 12 Nov 2008 Location: Bude, Cornwall Posts: 4014 |
New one to me, completely flummoxed:
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15th Feb 2015 3:44pm |
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stan Site Moderator Member Since: 13 Jul 2010 Location: a moderate moderated moderator moderating moderately in moderation Posts: 35267 |
wiring loom Dan? ... - .- -.
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15th Feb 2015 3:48pm |
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dan_uk_1984 Member Since: 12 Nov 2008 Location: Bude, Cornwall Posts: 4014 |
Thanks Stan, all looks good.
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15th Feb 2015 3:54pm |
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stan Site Moderator Member Since: 13 Jul 2010 Location: a moderate moderated moderator moderating moderately in moderation Posts: 35267 |
http://www.fullfatrr.com/forum/topic23644....aft+sensor
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15th Feb 2015 3:59pm |
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dan_uk_1984 Member Since: 12 Nov 2008 Location: Bude, Cornwall Posts: 4014 |
Unfortunately Stan, both of those posts have no resolution, I assume after Vento got the car fixed he left the forum
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15th Feb 2015 5:06pm |
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dan_uk_1984 Member Since: 12 Nov 2008 Location: Bude, Cornwall Posts: 4014 |
Got it booked in to a garage to get the crankshaft sensor replaced, will tow it with the other L322 following the towing procedure. |
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16th Feb 2015 9:34am |
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johnboyairey Member Since: 11 Jan 2013 Location: surrey Posts: 2032 |
the crankshaft sensor is a two minute job, two allen head bolts, and a connector. Then pull it out...i did mine at off road height, spare wheel under the sidestep, lay under step, and reached under. mine was stranded, so it was easiest option. as said, i needed a camshaft sensor, (another 2 minute job,) i couldn't find a secondhander, and new was an order in job, so i found that an ebay seller did them new for a m62 engine, but they had a male socket on, not the famale i needed, so as it was only £15 each, i solderered them to the old females, and ---VROOOM!
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16th Feb 2015 2:01pm |
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dan_uk_1984 Member Since: 12 Nov 2008 Location: Bude, Cornwall Posts: 4014 |
Unfortunately it turns out I have no compression on one bank - this means the valves are not operating as they should.
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18th Feb 2015 11:33pm |
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dan_uk_1984 Member Since: 12 Nov 2008 Location: Bude, Cornwall Posts: 4014 |
To follow up - the plastic timing chain guides (yes, plastic, Thanks BMW!) had failed and become snagged in the chain and ripped off, the chain was then allowed to move, which pretty much destroyed everything.
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5th Apr 2015 7:26pm |
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verydisco Member Since: 10 Dec 2009 Location: UK/US Posts: 2952 |
Sad to read this but thank you for the update l=Oo\________/oO=l l:OolΞΞΞΞΞΞΞloO:l
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5th Apr 2015 7:28pm |
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Prepros123 Member Since: 28 Sep 2014 Location: Cornwall Posts: 35 |
Had this happen to my last one. Timing chain jumped because of worn plastic guides. Is it feasible to have these changed as a preventative measure though I should imagine it's a PITA of a job |
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6th Apr 2015 7:48am |
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Starberg Member Since: 08 Jan 2015 Location: Karlskrona Posts: 70 |
Sorry to hear that mate!
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6th Apr 2015 8:36am |
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Prepros123 Member Since: 28 Sep 2014 Location: Cornwall Posts: 35 |
Mine happened at 160000 odd so no idea what expectation is |
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6th Apr 2015 9:14am |
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